ImageVerifierCode 换一换
格式:PDF , 页数:3 ,大小:14.97KB ,
资源ID:1018009      下载积分:10000 积分
快捷下载
登录下载
邮箱/手机:
温馨提示:
如需开发票,请勿充值!快捷下载时,用户名和密码都是您填写的邮箱或者手机号,方便查询和重复下载(系统自动生成)。
如填写123,账号就是123,密码也是123。
特别说明:
请自助下载,系统不会自动发送文件的哦; 如果您已付费,想二次下载,请登录后访问:我的下载记录
支付方式: 支付宝扫码支付 微信扫码支付   
注意:如需开发票,请勿充值!
验证码:   换一换

加入VIP,免费下载
 

温馨提示:由于个人手机设置不同,如果发现不能下载,请复制以下地址【http://www.mydoc123.com/d-1018009.html】到电脑端继续下载(重复下载不扣费)。

已注册用户请登录:
账号:
密码:
验证码:   换一换
  忘记密码?
三方登录: 微信登录  

下载须知

1: 本站所有资源如无特殊说明,都需要本地电脑安装OFFICE2007和PDF阅读器。
2: 试题试卷类文档,如果标题没有明确说明有答案则都视为没有答案,请知晓。
3: 文件的所有权益归上传用户所有。
4. 未经权益所有人同意不得将文件中的内容挪作商业或盈利用途。
5. 本站仅提供交流平台,并不能对任何下载内容负责。
6. 下载文件中如有侵权或不适当内容,请与我们联系,我们立即纠正。
7. 本站不保证下载资源的准确性、安全性和完整性, 同时也不承担用户因使用这些下载资源对自己和他人造成任何形式的伤害或损失。

版权提示 | 免责声明

本文(REG NASA-LLIS-0362-1994 Lessons Learned - Magellan Radio Transmitter A Modulation Failure.pdf)为本站会员(ideacase155)主动上传,麦多课文库仅提供信息存储空间,仅对用户上传内容的表现方式做保护处理,对上载内容本身不做任何修改或编辑。 若此文所含内容侵犯了您的版权或隐私,请立即通知麦多课文库(发送邮件至master@mydoc123.com或直接QQ联系客服),我们立即给予删除!

REG NASA-LLIS-0362-1994 Lessons Learned - Magellan Radio Transmitter A Modulation Failure.pdf

1、Lessons Learned Entry: 0362Lesson Info:a71 Lesson Number: 0362a71 Lesson Date: 1994-11-04a71 Submitting Organization: JPLa71 Submitted by: A.G. GussnerSubject: Magellan Radio Transmitter A Modulation Failure Abstract: Loss of Magellan telemetry data was traced to moisture contamination due to a subc

2、ontractors failure to use dry gas in the repackaging of an operational amplifier. Recommendations involve use of fault tree analysis, appropriate component screening and qualification, minimizing power cycling, and using dry gas.Description of Driving Event: After a star calibration during the Magel

3、lan third extended mission, the X Band telemetry and high rate data were missing from the down link (22 kHz and 960 kHz subcarriers were missing). A subsequent attempt to use the 360 kHz subcarrier also resulted in no significant subcarrier in the down link.The most likely failure is a HA 2520 opera

4、tional amplifier used as a summing amplifier in the telemetry signal conditioner (although a failure in the phase modulator circuitry is also a possible cause). It failed after 20,600 hours of flight operation and 2,600 power cycles (resulting in 10-15 degree thermal cycles). A prelaunch failure on

5、this component type indicated the possibility that during the repackaging process by the subcontractor of the HA 2520, moisture was trapped inside the electronic component. This moisture would combine with the phosphorus dopant in the glass passivation forming phosphoric acid that would enter throug

6、h pinholes in the passivation layer and attack the nickel-chromium resistors causing failure. The subsystem contractor did not use a dry gas during the repackaging process; instead air with a moisture content of greater than or equal to 5,000 PPM water was used. The prime contractor, with JPL concur

7、rence, felt that additional screening had been sufficient to identify any other faulty HA 2520 amplifiers.It was concluded that the in-flight failure may be related to stress induced by thermal cycles resulting Provided by IHSNot for ResaleNo reproduction or networking permitted without license from

8、 IHS-,-,-from on-off power cycling.As a result of this failure, the degraded transmitter B had to be used to return science data at a lower rate for the remainder of the mission.Additional Keyword(s): IC Manufacturing and PackagingReference(s): PFR #52621Lesson(s) Learned: 1. In-flight failures cann

9、ot always be conclusively analyzed using available telemetry data.2. Failure to qualify electronic components and assembly capabilities to mission environmental requirements (including numerous power/thermal cycles) increases risk.3. Power cycling can create thermal cycle effects on internal failure

10、 mechanisms for electronic components and assemblies.4. Not using dry gas in the repackaging process can allow moisture to be trapped inside electronic components (hermetically sealed packages with a cavity) and possibly create pinholes if they dont already exist. Water can also evolve from thermall

11、y induced decomposition of the epoxy die attach. Moisture could then combine with the phosphate glass to generate corrosive phosphoric acid that can make the electronic component inoperative.Recommendation(s): 1. Consider using a fault tree matrix during the design phase to identify critical telemet

12、ry parameters needed to analyze failures.2. Match component screening and qualification to the mission, including any expected significant thermal cyclic excursions.3. Minimize mission designed power cycling to reduce thermally induced stress.4. Use of dry gas with moisture content below 5000 PPM in

13、 repackaging electronic components is a must.Evidence of Recurrence Control Effectiveness: N/ADocuments Related to Lesson: N/AMission Directorate(s): Provided by IHSNot for ResaleNo reproduction or networking permitted without license from IHS-,-,-N/AAdditional Key Phrase(s): a71 Environmenta71 Part

14、s Materials & Processesa71 Test & VerificationAdditional Info: Approval Info: a71 Approval Date: 1995-01-23a71 Approval Name: Carol Dumaina71 Approval Organization: 125-204a71 Approval Phone Number: 818-354-8242Provided by IHSNot for ResaleNo reproduction or networking permitted without license from IHS-,-,-

copyright@ 2008-2019 麦多课文库(www.mydoc123.com)网站版权所有
备案/许可证编号:苏ICP备17064731号-1